View Single Post
      06-08-2023, 08:05 AM   #1
Tennis01
Registered
4
Rep
2
Posts

Drives: 2011 328i
Join Date: Jun 2023
Location: oregon

iTrader: (0)

I need help please...

e92 2011 328 i dropped off on trailer was getting crank no start looked as if there was some water damage watched a youtube video that explains how to jump terminal 37 38 39 because I was getting DME codes etc so I made jumper and car started but was blowing white smoke and gas what smells like was coming out the exhaust I'm being told that the car sat for about a year and I replaced the battery because it was also sitting in a pool of water about 4 in deep I drain the water of course used voltometr and tested all plugins and pins everywhere all of the sensors I replaced fuel injectors spark plugs and vanos solenoids camshaft sensor coil packs and then I got a really good deal on a new ECU,Cas,Key and once I plugged all that in the car fired up with super smooth idle car was still smoking like crazy but no gas coming from exhaust I let it run for about 45 minutes until it finally dissipated I closed up everything and decided to take it for a ride around the block when I pulled out of the parking lot smoke was blowing like crazy again but wasn't in limp mode/engine malfunction reduced power did a quick loop around the block with tons of smoke following me and quickly got it back into the parking lot to where it sits again I have a foxwell scanner and I am getting codes pertaining to master relay over voltage from the DME module that's after I took out that jumper wire when I was taking it around the block that jumper wire was still in I am a bunch of money into this car and all I want to do is drive it I'm almost sure of it that it's not a head gasket and I forgot to mention that the last owner told me that he broke off the oil pump housing bolt so before I did anything I backed out that broken bolt and replaced it with the same bolt about half an inch shorter which I don't think matters... also when I removed the jumper wire I was getting power back to 3738 39 terminal on fuse box and I felt that the overvoltage codes and stuff were due to that dumbass idea bypassing the DME or whatever that did right now the only codes I'm getting is DME Master relay and it cranks no start and sounds super healthy like it wants to start... I know this breakdown of what I know and have done so far is kind of all over the place but someone please help
Appreciate 0